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14 minute read
A Light Show at Sea
By PR1(AW) Jeremy Smith, VAQ-132
We finished our JTFEX work-up and sailed east to start our upcoming deployment. The carrier’s CO just had made an announcement on the 1MC. You hear him so often that you start not paying full attention to what he’s saying, but tonight’s message caught my attention. I heard him say, “This is the captain. We just made our final recoveries of flight operations, and now we are ready to go on deployment. We are going to have an ice-cream social. I want you to take a break and meet three new people tonight. Stick out your chest and be proud that you’re serving on the JFK. Captain out.” He might have said more, but I had heard what I wanted to hear.
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Moments later, our squadron XO and another officer returned from preflighting the alert EA-6B aircraft. When they entered the PR shop, they told us about a thunderstorm on the horizon. Have you ever watched a lightning storm from the flight deck of an aircraft carrier at sea? It is one of the most incredible things you ever will see. Having been in the Navy nearly 11 years, I had experienced some thunderstorms at sea, some near and some distant. The close ones can frighten you, but the ones that are at a distance are worth taking the time to go up on the flight deck to watch.
I looked over at my new airman, knowing he never had seen a thunderstorm at sea and said, “Let’s go— you can’t miss this.” We grabbed our float coats and cranials and headed up to the flight deck. It was a perfect night: dark as can be, with this amazing lightning storm approximately five miles away. You could see the stars above and the Milky Way, with the lightning flashing off in the distance.
It was so dark I couldn’t see the ladder or the catwalk, so I carried my cranial in my hand because it still had the dark visor attached. I was thankful someone had a flashlight and lit up the ladderwell so we safely could reach the flight deck. On the patio of the flight deck, the area near the landing area officer, I looked around to see what direction the thunderstorm was coming from. It was up forward, toward the angle. I
could see the lights from an aircraft overhead. Since “No,” they corrected me; “the captain said we were we were off the coast of Florida, I assumed it was an recovering the last of our aircraft.” airliner passing. I told the airman that the best place My first in a long list of mistakes was that I didn’t to see the storm would be at the top of the angle. With listen closely to what the captain had said; I had gotten our cranials in hand and me leading the way, we set off into the habit of tuning him out. Second, I didn’t take toward the 4-wire, unknowingly walking into the landthe proper PPE and gear with me to the flight deck. I ing area aft of the 1-wire. didn’t have a flashlight, and, since I work on day check,
The airman asked me, “What’s that light behind us?” I still had a dark lens in my goggles. I barely could see
I told him, “That’s the mast of the plane-guard the ladders on the catwalk or the obstacles around ship that follows us from time to time.” me, so I didn’t wear my cranial. My third and biggest
He came right back with, “No, not that light—that mistake was I didn’t pay attention to what was happenlight!” pointing at a row of green and red lights next to ing on the flight deck. I walked into the landing area the LSO platform. while flight operations were going on. No more than 20
Just then, I heard the air boss yell out on the 5- seconds later, an FA-18 trapped and caught the 1-wire. MC, “Clear the landing area; we’re recovering aircraft!” I had no idea just how far into the landing area we had
The “Oh s#@*!” factor kicked in. I ran outboard gone, but what I did know was I could have gotten both toward the foul line, donning my cranial as fast as of us killed. I could and heading back toward my shop with my The following day, I returned to the flight deck well before flight
I walked into the landing area while operations were called away. I flight operations were going on. wanted to reenact the night before, just to see how far we were into the landing area or to see if we had fouled the deck. I discovered we were at least 20 feet into the landing area. If nobody had seen us, we surely would have been killed. Float coats have minimal reflection tape on them, but the cranial provides twice as much reflective matePhoto by PH3 John E. Woods rial. If we had been airman in tow. Once we returned to the shop and wearing our cranials and the proper PPE, we might the adrenaline started to subside, I was able to think have been noticed much faster. about what just had happened. My first thought was I learned several lessons. Never assume that flight my airman and I could have been killed because of my operations are over. Don’t enter the flight deck withactions. I also could have caused damage or loss of an out proper PPE. Know your surroundings. Have a light aircraft. What was I thinking? I knew always to check with you when going on deck at night. Even though the my surroundings on the flight deck, but complacency person with you might have more time and experience almost killed me and another person. I talked with the doesn’t mean you don’t have to look out for yourself. guys in the shop about what had happened. I told them Awareness is the key to survival. I’d swear I had heard the captain say we just had recovered our last aircraft.
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Send BZs to: SAFE-Mech@navy.mil
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AN David Bowles and AE3(AW) Heather Evanger VFA-102
USS Kitty Hawk (CV-63) was preparing for night launches. A sense of urgency could be felt along the deck among the aircrew. The re-spot had not yet been completed, leaving precious little time for preflight checks. Rain just had stopped, leaving the deck wet and slippery. Water pooled between patches of nonskid, and a tractor driver and director struggled to maintain traction while spotting Diamondback 114.
This aircraft was being towed across the fantail in the landing area when the jet began to slip toward the port deck edge. The director stopped the move, regained control, and then directed the tractor driver to continue the move. The push was proceeding normally about 10 feet from the rounddown.
As the jet started moving aft, the plane captain (AN Bowles) was watching and waiting to prep the jet for launch. He was surprised to see the towbar’s attaching points break away from the nosewheel axle, causing the towbar to drop down into the rims of the
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nosewheel. The tractor lost positive control of 114.
A yellowshirt was looking at the jet’s port mainmount, ensuring safe separation from the scupper, and didn’t realize the towbar had disengaged from the tow points on the nosewheel axle. The wingwalkers were looking at the director, unaware that 114 no longer was attached to the tractor. Seeing the aircraft rolling aft toward the rounddown, AN Bowles decided the tractor would be unable to stop the jet’s movement. He promptly signaled for AE3 Evanger to apply the brakes. AE3 Evanger immediately applied the aircraft’s emergency braking system, stopping the jet two feet from the rounddown. The jet was then chocked, chained, and inspected. AN Bowles discovered both nosewheel rims were bent, downing the jet for launch.
AN Bowles’ quick and assertive actions saved an FA-18F Super Hornet and, more importantly, may have saved the life of AE3 Evanger.
AEAN Michael Reimann HSL-46 Det 4
While Cutlass 467 was turning on deck, awaiting an amber deck to remove chocks and chains to launch on a C-Profile FCF, AEAN Reimann noticed a small piece of FOD come off the right side of the helicopter. He immediately signaled the LSE for entry into the rotor arc and retrieved the FOD from underneath the aircraft. He took the FOD (a small piece of rubber from the black, main, rotor-blade bumper) to the maintenance shop to ensure 467 still was safe for flight. AEAN Reimann’s quick action and keen attention to detail ensured Cutlass 467 completed its FCF safely and that the FOD didn’t cause a hazard to the aircraft, personnel on deck, or to the ship’s RSD.
Airman Michael Luebke HM-14
While doing a daily inspection on an MH-53E, Airman Luebke noticed the alignment of the No. 1 engine’s centerisolation mount was off-center. Further inspection revealed metal-to-metal contact between the engine-isolation mount and the quick-engine-change (QEC) frame. He immediately notified maintenance control and QA.
During QA’s investigation, it was discovered the engine’s torque-shaft housing was misaligned by one bolt, causing the engine mount to be off-center. Airman Luebke’s strict attention to detail prevented a possible catastrophic failure of the QEC frame, resulting from undue
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stress caused by the misalignment.
Sgt. Flaten VMA-311 “Tomcats” (currently deployed to Al Asad Iraq)
Sergeant Flaten showed extreme attention to detail on the night of March 2, 2005, when he discovered a parachute-riser assembly for the ejection seat was installed wrong. Had this equipment been installed in an aircraft, the aircrew easily could have been led into thinking the improperly installed koch fitting and SEAWARS just were twisted. Had an aircrewman attached the riser to his torso harness, he would have put an unintentional twist into his parachute riser. This action could have resulted in serious injury to aircrew in the event of an ejection.
AM1(AW) Gary Garstin VAQ-139
Petty Officer Garstin was troubleshooting a popped flap/slat circuit breaker when he noticed substantial grease build-up around the gearbox of a squadron EA-6B. A flaperon cable also was chafing against an adjacent hydraulic line. Upon further investigation, it was determined that all but two strands of the cable were severed, and the hydraulic line nearly was sawed in half.
His attention to detail prevented the loss of flight-control authority and averted a possible mishap.
AD2(AW) Daniel Masaveg VQ-1
On Dec. 28, 2004, while deployed to Kadena AB, Japan, AD2 Masaveg discovered a fuel leak coming from the bottom of the No.1 engine. He was doing a daily inspection on an EP-3E at the time.
AD2 Masaveg notified the W/C 110 supervisor and QA. After opening the engine’s nacelle doors, “A” panels, and lower nacelle-access panels, he didn’t see any obvious leaks. Further troubleshooting by AD2 Masaveg, the W/C 110 supervisor, and QA concluded a low power turn was required to locate the source of the fuel leak. During this turn, fuel was seen leaking from the fuel manifold directly on the labyrinth seal. The No. 1 engine was shut down, the hard line was retorqued, and a second turn was performed to check for leaks. If left uncorrected, this problem likely would have caused an engine fire.
AD2 Masaveg’s technical abilities, attention to detail, and active troubleshooting skills aided in finding a potential fuel-fed engine fire that could have resulted in the loss of an aircraft and aircrew.
AD3(AW) Demacardo Williams VFA-87
During flight operations, AD3(AW) Williams noticed that an access door located under the port horizontal stabilator was open during the recovery of a squadron aircraft. He immediately notified the plane captain to signal the aircrew to go hands out, to prevent switching valve checks that would have caused the stabilator to hit the access door. He secured the open door and returned control of the aircraft to the plane captain.
His quick action and attention to detail averted potential aircraft damage.
Sgt. Wiggins VMFA-251
Aircraft 201, which just had come out of phase, needed a post-phase maintenance turn. Sgt. Wiggins began his pre-turn walk around per the checklist the way he had done at least a hundred times before. Prior to attaching the intake screens, he dove the duct for the No. 2 engine. He was moving through his standard procedures: counting the fan blades, checking the nose cone, looking for knicks or dents in the guide vanes and stators...again, all things that he had done many times before.
Sgt. Wiggins felt a very small “rough” spot on the back of one of the stators in the 7:30 position. He notified Maintenance Control and Quality Assurance.
An investigation revealed that a bushing had worn and seized, causing the joint between the inlet variable guide vane and the stator to become prematurely fatigued, which resulted in structural failure of the component. Had this gone unchecked for much longer, it would have certainly resulted in the IGV breaking off and being sucked into the compressor section.
Despite a heavy maintenance workload, Sgt. Wiggins did not take shortcuts. The result was that he saved an engine and possibly an aircraft and pilot.
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AD3 Brandon Joy HSL-44 Det 1
During a daily inspection, Petty Officer Joy found fuel leaking from the pressure-refueling panel on Magnum 447. He quickly investigated the problem and isolated the leak to the pressure gauge. AD3 Joy directed the defueling of the aircraft and made a more in-depth inspection. He noticed the gauge body was loose, tightened and reinstalled it, then refueled the aircraft with no further problems.
AD3 Joy’s superior technical knowledge and mechanical skills provided a mission-capable aircraft for armed helicopter missions in support of Straits of Gibraltar transit and Operation Active Endeavor.
LCpl. Chandler Bunting VMFA-533
LCpl. Chandler Bunting (MOS 6048 flight-equipment technician) was sewing intake covers for the squadron’s FA-18D aircraft. This particular night, he was the sole member of the night crew for his shop and was doing the right thing by wearing the required PPE for this activity: safety goggles. While sewing an exhaust cover, the needle of the sewing machine broke in half and sent the needle flying—straight toward his right eyeball. The needle came off with such force that it embedded in his safety goggles and actually penetrated the lens by one millimeter. The needle was aligned with his eye and would have ended up in his eyeball had he not been wearing the safety goggles. By following established procedures and doing the right thing, LCpl. Bunting saved his eyesight and prevented a serious mishap. His professionalism and attention to safety allowed him to continue working that night and accomplish the mission…safely. Everyone has seen the posters of the needle in the eyeball; hopefully, just as many people will see this picture of the needle in the safety goggles.
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AD1(AW) Michael Shealy VFA-87
While serving as the line division LPO Oct. 4, 2004, Petty Officer Shealy distinguished himself through exemplary performance and unwavering dedication to duty. During flight operations at NAS Oceana, in support of unit-level training, he noticed
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a drill bit laying on the ground in the fire lane of the War Party flight line. He then searched the immediate vicinity and found four more drill bits on the ground. He immediately notified maintenance control, and flight operations temporarily were suspended while a combat FOD walkdown was held. A quick assessment revealed the source of the hard FOD was a flight-line vendor. The wing was notified, and squadrons at NAS Oceana were alerted to the potential FOD hazard that existed on their flight lines. His quick and decisive actions and attention to detail averted potential damage to the War Party aircraft. If left unnoticed, the drill bits could have caused catastrophic damage, costing thousands of dollars and lost sorties. His acute attention to detail during high-tempo and high-visibility flight operations highlights his commitment to excellence through professionalism and safety.
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AM3 Aaron Fugate HSL-44 Det 1
During a 56-day special inspection on Magnum 447, Petty Officer Fugate noticed what appeared to be a crack in the sealant on a main-rotor tip-cap. Investigating further, he carefully removed the sealant and found that the tip-cap was cracked and needed replacement.
AM3 Fugate’s meticulous attention to detail and thoroughness ensured that Magnum 447 was available to conduct assigned missions in support of Operation Iraqi Freedom in the Northern Arabian Gulf. His efforts prevented damage and a potential mishap.