Project 20 final ame poster 20 zy

Page 1

Stator Build Process Lean-Out

Grant Brann & Julie Shindler Dr. Harold L. Stalford

Chase Kovach & Ramon Torres Dr. Janet K. Allen

Sponsor Advisors: David Seaman & Syed Jamel

PROBLEM BACKGROUND

IMPROVEMENTS

ANALYZE

AUTOMATION

VALUE ADDED ACTIVITIES

• The stator press operation is performed to prevent the stator from rotating when used in downhole operations. • The stator press machine applies a compressive force to the lamination stack resulting in the laminations being in tension with the stator housing so no rotation can occur.

VAR =

Stator

Total Value Added Time 8.07 min = = 7.77% Total Process Time 103 min

IMPROVEMENTS

• The stator press process is currently manual labor Pressed intensive, except for the machine sub-process.

LAYOUT

Laminations

• Reorganize working area and update CAD Model

• Stators are assembled into motors used in down hole oil and gas drilling operations.

PARALLEL PROCESSING CURRENT—1 Technician

SET UP

PROBLEM DEFINITION

STACK LAMINATIONS

INSPECT SLOTS

PRE-MACHINING

SET UP

• Provide complete Process Documentation

DMAIC APPROACH

INSPECT SLOTS

SET UP

STACK LAMINATIONS

SET UP

STACK LAMINATIONS

INSPECT SLOTS

PREMACHINE MACHINING

SYSTEM IMPACTS SPONSOR’S GOAL: 30%

Analyze the System

• Identify value-adding activities

Improve the System

• Process Time, Throughput, Quality, Ergonomics

Control the System

• Update process documentation

PROCESS TIME 21%

CURRENT

PROPOSED

PROCESS IMPROVEMENTS 43%

TIME STUDY

BREAKDOWN OF IMPROVEMENTS Layout

TOTAL TIME

1

Set-Up

4 min 48 sec

2

Lamination Stacking

24 min 47 sec

3

Slot Inspection

7 min 8 sec

4

Pre-Machining Process

36 min 19 sec

5

Machine Operation

8 min 4 sec

6

Post Machining Process

22 min 8 sec

• REDESIGNED INSPECTION TOOL

Parallel Processing

17%

New tool design allows for the Inspecting and Stacking sub-processes to be combined 5% PROCESS THROUGHPUT QUALITY ERGONOMICS PROCESS TIME THROUGHPUTQUALITYERGONOMICS

1 hour 43 min

TIME

FINANCIAL ANALYSIS Initial Investment Savings IRR

STACKING TIME 3 mins 24 secs

Automation

21%

449 min = 49.89 minutes 9 stators

Average = 68 s/ft

Tooling

35%

TAKT TIME

3 ft

IMPROVED VAR FROM 7.77% TO 9.02%

QUALITY 5%

• SPLIT-THREAD BOLT TIGHTENING/UNTIGHTENING

MEASURE

TAKT TIME =

EXCEEDED SPONSOR GOAL BY 50%

THROUGHPUT 17%

TOOLING

TOTAL PROCESS TIME

POSTMACHINING

POST-MACHINING

PRE-MACHINING

Measure System Performance • Time Studies, TAKT Time

NAME

POST-MACHINING

• Organize carts by model rather than by tool type

• Process is labor intensive

SUBPROCESS

MACHINE

PROPOSED—2 Technicians

• Generate 30% Improvement in Stator Press Process

Define the Problem

Lowering and Positioning of Clamps

Mandrel Storage Racks

32 ft 36 mins 16 secs

INSPECTION TOOL

PROPOSED DESIGN

$34,600 $64,826 53%

Improvement Cost New Inspection Tool (6) $18,000 Carts (2) $800 Mandrel Automation $800 Clamps Automation $15,000 Total $34,600

IMPROVEMENTS ALLOW FOR 350 MORE STATORS TO POTENTIALLY BE PRODUCED A YEAR


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